广州建筑 ›› 2021, Vol. 49 ›› Issue (3): 33-.

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某风井深基坑渗漏水处理加固方案及施工技术

  

  • 出版日期:2021-06-01 发布日期:2021-07-19

Reinforcement Scheme and Construction Technology for Leakage Treatment of Deep Well Foundation Pit

  • Online:2021-06-01 Published:2021-07-19

摘要: 某区间风井深基坑在土方开挖时发生了渗漏,渗漏点深度约32m,涌水量大,在采用MJS工法桩和WSS注浆方法达不到加固效果后,最终选用了在基坑东西两侧采用水下低标号抗渗素混凝土墙与原端头加固素混凝土墙形成包围后再注浆加固的方法,采用该方法进行加固处理后,通过声呐法测出的素混凝土外侧测孔的流速、流量值明显小于混凝土地连墙外侧(素混凝土墙内侧)测量孔的值,且素混凝土墙外侧21个测量孔平均流速值均小于6.0×10-6cm/s,可见基坑外侧素混凝土墙起到了预期加强止水的效果;通过示踪试验和微水试验显示加固后土层的渗透系数在10-4cm/s数量级,加固效果明显,且周边降水效果明显改善。风井基坑经加固处理后,在重新开挖过程中未发生涌水涌沙情况,并顺利地完成了风井底板结构的施工,证明该加固方案有效。

Abstract: Leakage occurred in the deep foundation pit of an interval air shaft during the earth excavation. The depth of the leakages is 32m and a great deal of water busted immediately. Firstly, the Metro Jet System (MJS) and WSS methods can not achieve the reinforcement effect. Finally, the method of grouting reinforcement is adopted after the surrounding of underwater low-grade impermeable plain concrete wall and the original end reinforced plain concrete wall is formed on the East and west sides of the foundation pit. After the reinforcement treatment with this method, the velocity and flow value of the measuring hole outside the plain concrete measured by the sonar method are obviously smaller than those of the measuring hole outside the reinforced concrete diaphragm wall (inside the plain concrete wall), and the average velocity values of the 21 measuring holes outside the plain concrete wall are less than 6.0 × 10-6cm / s, it can be seen that the plain concrete wall outside the foundation pit has the expected effect of strengthening the water stop; The tracer test and micro water test show that the permeability coefficient of the soil layer after reinforcement is in the order of 10-4cm / s, the reinforcement effect is obvious, and the surrounding precipitation effect is obviously improved. After reinforcement, no water and sand gushing occurred in the process of re excavation, and the construction of air shaft floor structure was successfully completed, which proved that the reinforcement method was effective.